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Control Loop Case History 101

Loop analysis uncovers problems

One of the greatest fallacies that exists in so many process plants is that tuning will sort out all the problems.  As soon as a control is not working properly the cry arises from the process people that the loop needs tuning.  In most cases the C&I maintenance people send out a person who might spend quite long time playing with the tuning trying to improve things.  He or she seldom tries to analyse the loop, which consists of:

  1. Understanding at least the basics of the process.
  2. The purpose and importance of the control.
  3. The required speed of control response.
  4. Possible external effects that could affect the process.
  5. Process stability.
  6. Establishing the dynamics of the process, and if these could change with time or differing conditions.  This is vital for correct tuning.
  7. If the valve and transmitter are correctly installed and calibrated right.
  8. Checking for possible problems including incorrect or poor control strategy, possible measurement problems, and if there are any difficulties associated with valve problems (which is where 90% of loop problems do occur).

This Case History is going to give two examples of cases where I have been called in to “tune the loop” and some simple analysis has shown up severe problems.

The first is a very simple example, and is of a temperature control loop in a chemical plant which has always had to be run in manual.  Many people have unsuccessfully tried to tune the controllers.

Luckily the control consisted of a cascade system with the output of the temperature controller connected to the setpoint of a flow controller whose output was connected to the control valve.  I say “luckily”, because as pointed out in a recent Case History, it is very much easier to analyse valve behaviour if one can measure the flow through it.  The open loop flow test on the secondary flow loop is shown in Figure 1.  

Fig. 1

The test shows clearly that automatic control is absolutely impossible with this valve when comparing the controller’s output signal and the flow through the valve(hence valve position).  There is virtually no correlation between the two.  At times there are huge overshoots on step changes with slow return to the correct position.  On occasion the valve actually moves in the reverse direction to that of the change on the controller’s output signal.

If one had not been able to access the information given by the flow test, and if the temperature controller had been connected directly to the valve, as so often happens, it would have been extremely difficult if not almost impossible, to try and find out why one could not achieve control.

I do find it amazing that the Operators were able to run this loop at all taking into account that the valve was effectively working virtually completely “independently” to the controller.  I also find it even more amazing that this problem had not been picked up much sooner, and that people were wasting hours of time trying to tune the controller.

The second example is extremely interesting.  I had been asked to try and tune a controller, the purpose of which was to control the furnace pressure of an arc furnace.  This is normally a very difficult loop to optimise as arc furnace pressures tend to jump about quite considerably.  People often say they are “unstable”, which is not a correct statement. 

Conditions inside the furnace are very non-consistent, which causes the pressure to move around in an intermittent fashion.  Also the pressure transmitters are normally calibrated over a very small pressure range, typically –5 to +5 mBar.  This is really tiny, and it amplifies the pressure variations over quite a large percentage of the tiny range of the transmitter.

For various good reasons the process specialists would like to control these furnaces at a slightly negative pressure.  Many people think that the pressure control system should be capable of instantly taking care of all the fluctuations.  This of course is impossible.  The variations occur due to sudden and non-repeatable changes internally in the furnace, and it would be impossible for any feedback control system to try and catch them.  In my way of thinking, the changes must be classified as “noise” which we can define as random fluctuations in the process variable signal around a mean level.  The control must be set-up so that it smoothly controls the average pressure, but must be fast enough to also catch sudden large load changes, which can for example occur if a feed does suddenly change drastically.

In the example under discussion the furnace pressure control had been a major problem for many years.  The furnace was tripping regularly mostly due to high pressure trips, and a lot of production was being lost, as it takes quite a long time to restart the furnace after a trip.

To analyse a loop, the most important test is the open loop test, where one makes changes on the output of a controller (that is in manual), and try to ascertain from the recordings information like valve performance and process dynamics.

In the case of this furnace we tried running this test over a period of a day and a half, with very little success, as the noise (random changes) in the furnace pressure were so large and numerous that it was almost impossible to really get any repeatable and reliable information from it.

When performing this test four signals were recorded:

  1. Controller output (PD)
  2. Furnace pressure
  3. Valve feedback position (as the valve was operated by an electric actuator)
  4. Flow through the valve

It was extremely useful to have the last two signals which gave quite a bit of useful information.  Firstly comparison of the valve feedback position with PD showed that the valve was following the PD extremely well, and also moved very quickly.  This allayed a worry of the client who had been advised by the furnace manufacturer that a possible reason for the poor control was that the valve was moving too slowly.

Secondly a comparison of the flow versus PD showed that the flow was saturating (reaching a maximum) about half way up the range.  This can be seen in Figure 2.   

Fig. 2

If we had not had the valve feedback signal it could have meant that the valve was not moving past a certain position, and it would have meant conducting tests on the valve itself.  However knowing that it was in fact moving well meant looking for a reason for the flow saturation elsewhere.

There could have been several reasons for it.  One could have been that the extraction fan device which sucked the gases out of the furnace could have problems, and could not deliver sufficient volume.  Another could be blockage somewhere in the system.  However the most likely reason was due to the fact that the gas was finally passed through water seal tanks before it was sent either to a storage tank, or else to stack.  It was felt that the levels in the seal tanks were too high and were causing a big back-pressure upstream.

A test was performed where the levels in the tanks were lowered slightly.  The flow of gas immediately increased.

Unfortunately it is beyond the scope of this article to delve too far into the workings of this system, but recommendation were made to the client as to proper control of the tank levels and to operate the tanks at lower levels, which would surely alleviate many of the problems being experienced.

The important lesson to be learnt from the exercise though is how important it is to analyse all the information available in order to solve problems.  Once again if the flow signal had not been available it would have been very difficult and most probably would have taken a lot longer to find what was causing the problem.  

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Michael Brown is a specialist in control loop optimisation, with many years of experience in process control instrumentation. His main activities are consulting, and teaching practical control loop analysis and optimisation. He gives training courses which can be held in clients' plants, where students can have the added benefit of practising on live loops. His work takes him to plants all over South Africa, and also to other countries. He can be contacted at:
Tel (011) 486-0567
Fax (011) 646-2385
E-Mail: 
michael.brown@mweb.co.za