Control
Loop Case History 117
Control
Problems in a Chemical Plant
I was recently performing some optimisation in a
large chemical plant. In the daily hustle and bustle and general
high pressure on an instrument and control practitioner, one can
easily forget some of the basics. When a problem arises in a
loop, many people try and solve it quickly by adjusting the
controller tuning, which of course is the very last thing that
should be done. You need to always analyse the loop first, and
many of my previous articles have dealt with this.
I have found on quite a few occasions that the last
thing that many people look at is the measurement even though
the first law of control states: "You cannot control what
you don’t measure". On one memorable occasion (which I
did describe in an early Case History article) an instrument
technician tried tuning a controller for over 6 hours, only to
find later on that the problem was actually blocked impulse
lines between the orifice plate and the transmitter.
The first example here is a similar type of thing
where a measurement technique was being incorrectly employed. A
flow was being measured using an ordinary concentric orifice
plate and d.p. (differential pressure) cell. The control was not
working well and operators were running the loop in manual.

Fig 1
Figure 1 shows an open loop test that was performed
on the loop. At first glance it would appear that there is a bad
valve problem as the controller output is initially being
stepped around quite a bit, but with no corresponding changes in
flow. However the people working on this loop had completely
forgotten the basics of orifice plate measurement.
This method of flow measurement is one of the
oldest and best established having been around since the 18th
century. Basically there is a well known relationship between
the flow through the orifice, and the differential pressure
across the orifice. This method of flow measurement is not very
accurate, being typically quoted by a British Standard as ±2%
of full scale, over a rangeability (maximum to minimum flow) of
3:1. Over the decades most control people accept that an orifice
measurement can in fact be used with good repeatability over a
4:1 rangeability, even though the accuracy will be very bad at
the 25% lower end of the scale. However the readings below that
must be assumed to be absolutely meaningless, and should never
be used or relied on.
In this case the plant was trying to control the
flow at less than 10% of the measuring range. This is impossible
with the current measurement setup. There was really no more
point in doing any more work on the loop until the measurement
problem was sorted out.
Another example of a measurement problem in the
same plant was on a steam flow where it was important to keep
the steam flow exactly on a certain setpoint. However the flow
seemed to be oscillating wildly at maximum range and could not
be reduced. This is shown in an open loop test as seen in Figure
2, where the output of the controller is being stepped down with
no corresponding reduction in steam flow.

Fig 2
On inspecting the plant it was found that the
orifice plate installation was faulty, with no condensate pots
installed, and 2 phase flow was probably passing through the
orifice.
The third and last example in this article, was of
a case of a very poor control strategy employed on a heat
exchanger.
Figure 3 shows the setup. It is a pretty standard
temperature to flow cascade control system employed often on
heat exchangers, but with one exception. This was that the valve
was not in series with the pump, but was bypassing the fluid
used to adjust the temperature from the pump’s output back
into the vessel. This was probably to prevent too small a flow
through the pump, which may have damaged it.

Fig 3
The operators were complaining that the control was
useless as it was impossible to bring the temperature of the
process fluid to setpoint. In most plants when controls aren’t
working everyone assumes that the controller tuning is wrong. So
as usual, quite a few people had tried to retune the
controllers, but with no improvement.

Fig 4
Figure 4 shows the open loop test done on the flow
loop. It can be immediately seen that stroking the valve between
0 and 100% could only result in the flow changing between a
minimum of 32% and a maximum of 40%, a measly range of 8%.
Obviously the differential pressure across the valve, even when
fully open is much less than the pressure drop downstream of the
pump across the heat exchanger. If this was the reason that the
bypass valve system was employed, then the best solution to the
problem would be to incorporate another valve in series with the
heat exchanger, and to use split range control to ensure that
the flow to the heat exchanger could be modulated fully over the
whole 0 – 100% range, whilst still ensuring that the pump
always has sufficient flow through it to prevent damage.
The revised strategy is shown in Figure 5.

Fig 5
If one did not use identically sized valves, then
special precautions must be taken to ensure that the process
gain remains constant across the whole range. If not adaptive
tuning could be employed. This has been discussed in other
articles.
The examples given in this article once again show
important it is to fully analyse all components of a control
loop, and to understand the control requirements before trying
to tune the controller.
Index to articles
Michael Brown is a specialist in control loop optimisation, with many years of experience in process control instrumentation. His
main activities are consulting, and teaching practical control loop analysis and optimisation. He gives training courses which can be
held in clients' plants, where students can have the added benefit of practising on live loops. His work takes him to plants all over South Africa, and also to other countries. He can be contacted at: Tel (011) 486-0567
Fax (011) 646-2385 E-Mail: michael.brown@mweb.co.za
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